Thursday, September 10, 2015

SkyView Anomaly

This morning I went flying for a short hop around the valley.  I took off from U42 and did a touch and go.  I then headed south and then east flying over South Jordan and then north over Sandy.  I flew up to SLC and then turned south and flew along the foothills to Draper.  I flew over Corner Canyon into the Alpine area.  I then turned west and flew south of the Micron site and then turned north at the Point of the Mountain and at the bend of Bangerter I headed west towards Herriman and then north to land at U42.
When I was about 5 miles from the airport a strange thing happened to the SkyView screen.  On the PFD portion of the screen there was a narrow band of synthetic vision with the top and bottom of the PFD display blacked out.  It stayed that way all of the way to the ground.  The data remained visible but the synthetic vision was virtually gone.  After landing and taxying to the hangar I called Dynon.  They asked me to send them some photos of what I was seeing.  
I sent these photos to Dynon.  The first photo shows the PFD, EMS and MAP all displayed.  The next 2-photos show that when the PFD and EMS is displayed the synthetic vision is not correct.  Also, when the PFD is displayed alone the synthetic vision is correct.  Dynon’s response was, The issue you reported (black background on your PFD) is apparently a known issue that is being investigated by our engineering team. Hopefully it will be fixed in an upcoming firmware release.”  I have asked Dynon if this means I should not fly until a fix has been provided or if it is OK to fly with the SkyView as is.  I am still waiting for an answer.

Wednesday, September 2, 2015

SV-KNOB-PANEL CONTINUED

Today I finished the installation of the auto pilot control module.  I drilled and countersunk the holes for the nutplates then cut out the panel with my Dremmel tool.  I had to file the opening slightly to get the module to fit in the opening.  I installed the nutplates using some flush pulled rivets.  
I installed the module and powered up the system.  I had to have SkyView find and then configure the SV-KNOB-PANEL.  After the set up was complete I turned on the SkyView system and it was there.  I was able to set the altitude and heading bugs as well as adjust the Barro.  I closed the hangar doors and checked to make sure the backlighting is working.  It is and now the unit is ready to go flying.
After installing the new placards I decided to try out the panel.  I got the airplane out and did a pre-flight.  I got in, started the engine and went up for a quick flight.  I did a couple of touch-and-goes then headed south to Herriman.  I flew over Herriman then headed north.  The wind at the time was reported 150o at 18kts with gusts to 22kts so it was a little bumpy flying over the foothills west of the airport.  I flew up to Magna then noticed a big dust cloud east of Antelope Island.  I decided to head back to U42 in case it was heading south.  While flying over Harriman and then north to Magna I turned on the autopilot.  All of the functions work perfectly.  It is nice to be able to adjust the barometer, altitude and track/heading without selecting these functions first on the SkyView menu.  
All in all this is a really nice feature and I am glad I installed the panel.

Friday, August 28, 2015

SV-KNOB-PANEL

I decided to install the knob panel for the SkyView.  I purchased the panel from Dynon.  Of course I didn’t stop to think it would require a harness to hook it into the system.  After the device arrived I realized what happened so I ordered the harness.   It is due to arrive this afternoon.  In the mean time I have removed the upper fuselage skin, radio and the large information placard from the instrument panel.  
I also used some blue tape to outline the location of the new control panel.   I removed the SL40 radio and the information placard above the radio.  I will redo the placard so it is not so wide.  I am also going to reduce the height of the 'final check list' located above the corner of the D1000 panel.  It is partially covered by the canopy bar when the canopy is closed.
I also ordered some MK2000-6 nutplates from Aircraft Spruce.  
I taped some plastic on the instrument panel and inside of the cockpit to keep the aluminum shavings from drilling and cutting from getting into everything.  I will use the small vacuum to help keep the debris under control.  After the nutplates arrive I will determine if the layout on the template is the correct spacing for the nutplate holes.  At that point I can start drilling and cutting the panel.  I will drill the panel first for the nutplate and mounting fasteners.  I will then use my Dremel tool to cut out the opening for the control panel. 

Tuesday, June 16, 2015

Flight to Kanab, UT

Today I flew to Kanab with my granddaughter, Taylor, as my copilot.  We had a really fun trip.  We left SVR at 9:00 am and flew to Kanab arriving at 11:30 am.  It was a fairly smooth ride.  We hit a little bit of turbulence over the mountains south of Panguitch, but otherwise a pretty nice ride.  When we got to Kanab we checked in with Jeff Turner, the airport manager and borrowed the courtesy car and drove over to hour house in the Kanab Creek Ranchos.   Our house is located almost directly west of the north end of runway 19.  You have to do a little wondering around to get there.  Because there are only 2-places to cross over Kanab Creek there is not a direct route.  We went to the house and then Taylor drove us to Subway for lunch.  After lunch Taylor drove us around town and then we went back to the airport.  We took off for home at 1:00 pm.  The wind was 190o at 13.  We took off on runway 19 then circled the Ranches gaining altitude.  After reaching 7500’ we headed north.  Because of the wind and thermal activity it turned out to be a pretty bumpy ride all the way up to the Salt Lake valley.  We arrived at SVR at 3:30 pm.  It was a fun day, and because Taylor had her cell phone and I had a MP3 player she was able to listen to music almost the entire trip down and back.  She was a happy flyer. 
These are photos of the airplane parked at the Kanab airport, a photo looking west towards the Ranches and a picture of the terminal at the airport.

Tuesday, March 24, 2015

Hangar Visit

On March 11th I had several young men (Varsity and Venture Scouts) and their leaders come to the hangar for a visit.  Actually, several of these young men saw the airplane during the time it was located in my garage.  Since it is now finished and flying they thought it would be fun to come out and see it in its new home.  
They spent about an hour looking around the hanger, the airplane, sitting in the airplane and asking questions.  The leaders also participated and all seemed to have a good time.  Below are some pictures taken by Ivo Stutznegger, a good friend and one of the leaders of these young men.
We took off the upper cowling so they could see the engine.
Some of them wanted to sit in the cockpit.
I think everyone had a good time.  Maybe there are some future pilots in the group.

Tuesday, March 10, 2015

Finish Blast Tube Relocation

Today I finished the installation of the blast tube.  The epoxy resin cured overnight so I took the lower cowl out to the hangar.  I took a picture of the airplane with the lower and upper cowls off.
I installed the lower cowl making sure the oil cooler lined up correctly and the control for the oil cooler shutter was inserted into the guide tube running through the cooling duct.  I bolted the oil cooler shutter in place along with the oil cooler.  I hooked up the controls to the oil cooler shutter and the duct damper door.  I inserted the end of the blast tube into the fitting and tightened the screw clamp.  I also clamped the scat tube to the lower cowl opening.  Everything went together just as it was supposed to.  I moved the airplane out onto the apron and started the engine.  It started and ran fine.  I put the top cowling on and went up for a test flight.  It went well.

Monday, March 9, 2015

Blast Tube Relocation

I continue to see posts in VansAirForce form about voltage regulators failing.  I have printed off the recommendations for testing the system if the regulator seems to be out.  In addition I have been thinking about a better way to cool the regulator.  My thoughts are that if the blast tube from the shroud on top of the engine were relocated to the cowl duct it might provide a cooler air supply.  Also, if the attachment to the cowl duct is made so it is a scoop in the airstream it may improve the cooling effect.  I may be all wet, but I decided to try it out.  
For the scoop I purchased a ½” – 45o PVC slip fitting.  I removed the upper and lower cowlings.  I also disconnected the blast tube from the engine cooling shroud.  I inserted a plug and put RTV over it to seal the plug in place.
I drilled a hole in the top of the lower cowling duct tunnel about 6” in front of the damper.  I used JB Quick Weld to attach the slip fitting to the cowling.  I cut the end of the fitting into which the blast tube will fit with the band saw.  I cut the fitting so a screw clamp can compress the end of the fitting and hold the blast tube in place.  I put RTV around the end of the blast tube for a good seal to the fitting.  Now when the end of the tube is placed in the slip fitting and the clamp tightened it will not pull out.
I then mixed some epoxy resin, cut some fiberglass and laid up some fiberglass over the fitting to secure it to the cowling.  I put fiberglass on both the top and bottom of the fitting where it goes through the upper wall of the duct.  I will let the fiberglass cure overnight and reinstall the cowlings and connect the blast tube tomorrow.



Friday, January 23, 2015

Fly to Wendover

This morning I fueled the airplane with 10 gallons of premium and took off for Wendover.  I climbed to 5900’ as I departed the cross wind leg from runway 34.  As I flew over Magna I uploaded a flight plan and engaged the autopilot in the HSI & ALT mode.  As I flew over the Salt Air Resort I started my climb to 7500’.  As I arrived over the evaporation ponds north of Grantsville I climbed to 8500’.  I flew to Wendover over the Bonneville VOR.  I landed in Wendover and parked on the ramp. 
There were 4-other RV’s parked there.  An RV-7, an RV-6, and RV-8 and an RV-7A. There was also a Cessna 152 which had taken off from South Valley Regional about 20 minutes before I did.  I went inside and purchased an Historic Wendover Airfield cap.  I then got back into the RV-12 and flew back to South Valley Regional.  My trip out took 1.2 hours.  My flight back was 1.1 hours.  It was a great day to be in the air.  Upon my return and purchased another 10 gallons of fuel and put it in the tank.  As I finished fueling the Cessna 152 I followed to Wendover entered the pattern and landed.  It is a small world.  I hope to go up again next week.

Wednesday, January 7, 2015

Carburetor Float Buoyancy Test

Yesterday and today I worked on testing the carburetor floats as required by the ROTAX Service Bulletin – SB-912-065 R1.  I believe the serial number of my Rotax 912 ULS engine is out of the range of engines which need to be tested but I am complying with the test anyway.  Two weeks ago I ordered new choke gaskets for the carburetors.
Yesterday I removed the upper cowling.  I also prepared a 60 ml syringe by attaching a section of ¼” hose to the end.  I safety wired the hose to the syringe.  Today I modified a section of oil spout from an oil bottle to make a fitting which will go into the port on the carburetor.  I then moved the airplane out onto the apron and closed the hangar doors.  I started the engine and let it run for 2-minutes to ensure the carburetors were full of fuel.  I pushed the airplane back inside and proceeded to perform the test on the left carburetor.  I removed the choke spring and vent tube.  I removed the 4-screws holding the choke assemble to the side of the carburetor.  Using the syringe containing 60 ml of fuel I injected fuel into the lower port until it began coming out of the vent tube.  It took 25 ml’s of fuel.  The range of fuel volume for filling the float chamber is  23- 40 mls.  Any amount less or more indicates a problem.  The left carburetor is acceptable.  I reinstalled the choke assembly, vent tube and spring.  I then repeated the process on the right carburetor.
Both the left and right carburetors are acceptable.  They both required 25 mls of fuel to fill the float chambers. After putting everything back together including the upper cowling and putting the 5-gallons of gasoline I purchased into the tank I decided to go up for a test flight.  It was a beautiful day for the 7th of January.  The temperature was 54o F and the winds were light out of the south.  I took off on runway 16 and made 4-touch-and-goes.  The engine continues to run great!  I landed and put everything away.  I brought the engine log book home and made an entry certifying that Rotax SB-912-065 R1 has been complied with.