Today I went flying before the bad weather
hits. It was fun to just fly around the
pattern and do some touch-and-goes. I am
learning just where to set the trim to hold 60 knots and descend from pattern
altitude to the runway. I am zeroing in
on the technique to have good landings each time I come around. I removed the rear portion of the nose wheel
pant and dropped it off for Dave to paint.
I hope he is able to get to it soon.
Monday, July 28, 2014
Thursday, July 24, 2014
No Problems With Repaired Wheel Pant
I reinstalled the aft portion of the nose
wheel pant and went flying yesterday and today.
I made a total of 7-take-offs and landings with no problems. The wheel pant is just fine. I will remove it from the airplane and take
it to Dave Wissinger on Monday the 28th.
Tuesday, July 22, 2014
Completed The Wheel Pant Repair
Today I completed the repair of the nose
wheel pant. I laid out and cut the
opening for the tire. I enlarged the
opening to the rear so I would not have a repeat of the earlier problem. I sanded the fiberglass resin and then
applied some body filler over the voids.
I sanded the body filler and the pant is now ready for paint. I left a message for and then texted Dave
Wissinger to let him know it is ready to be painted. Dave is heading out of town today and will be
back this weekend. I told him I would
get the pant to him on Monday and he said he would get it painted. What more can I ask for? I will put the pant back on the airplane and
go flying. I will remove it and take it
to Dave on Monday.
Monday, July 21, 2014
Resume Wheel Pant Repair
I went to the airport today and sanded the
fiberglass patch I put in the wheel pant last week. I then added an additional layer of
fiberglass to the inside of the repair area and put a layer of epoxy resin over
the patch on the outside. Tomorrow I
will return and sand everything down. I
will probably have to use some body filler to fix any small voids in the
surface.
I also attached a carbon
monoxide monitor card to the instrument panel.
Wednesday, July 16, 2014
Repair Nose Wheel Fairing
Yesterday I discovered the bottom of the rear
portion of the nose wheel pants had been broken out. I removed that portion of the pant this
morning to fully survey the damage. It
appears from the black on the corner that was broken out that I need to extend
the rear opening a bit more to the rear of the pant.
I cut a piece of blue foam to make a form for
the shape of the bottom of the fairing.
I carved and sanded the foam to the proper shape than covered it with
plastic. I also marked where the original
cutout for the wheel was located.
I cut some fiberglass patches. One to go over the blue foam with the edges
to the inside of the hole. This piece will
be sort of a filler. I then cut a piece
that will go over the entire hole out to where I have sanded away the white
paint. I mixed some fiberglass resin, saturated the pieces and
put them in place on the fairing. I will
allow this setup to cure and then remove the foam and put another layer of
glass inside of the fairing.
Tuesday, July 15, 2014
Went Flying
Today I went flying. I took off and everything went perfect. I did 2-touch and goes at South Valley
Regional then headed NW to the Tooele valley.
I did 2-touch and goes at the Tooele Valley airport and then headed
south to Cedar Valley. I engaged the autopilot
and climbed to 7500’. I flew around the
Munitions Disposal Plant and then west.
I flew into a across Cedar Valley then to the east side of the Lewiston
Peak and up the shore of Utah Lake back to the point of the mountain. I entered the Salt Lake valley and flew NW to
South Valley Regional. I made one last
landing then put the airplane away.
While doing so I noticed a sort of clicking sound coming from the nose
wheel. I checked and found the nose
wheel fairing had been broken. I don’t
recall flopping the nose wheel on any of my landings but it obviously deflected
enough to catch the rear and sides of the fairing and it broke out a chunk about
3-4” behind the tire. I will remove the
back portion of the fairing and do a fiberglass patch. I will then take the fairing to Dave
Wissinger and have him repaint the lower portion of the fairing. I guess there will always be something to
work on.
I took some new photos of the
airplane. I need to come back and take
better photos in the afternoon sun.
Monday, July 14, 2014
Ready To Fly
We returned from our trip to
San Luis Obispo, California.
Arlene’s aunt passed away and we decided it was important for us to be
there. Other than her son and his wife
and her daughter, we were the only family members in attendance. Aunt Ruth was 95 years old and most of her
friends have already proceeded her in death, so the funeral was quite
small. Arlene and I have not been in San
Luis Obispo since 1971. I went to
college at Cal Poly and it was fun to see the old campus again. It has changed drastically in the last 43
years. I even found a dorm building with
our name on it. I am sure it was not named ‘Jespersen Hall’
because I attended school there. But, it
was fun to see and I took a picture.
Today I put the top cowl back on and adjusted the fuel computer to
a more realistic number. I took a
picture of the reinstalled and sealed pitot tubing attached to the pitot
tube. It also shows the safety wire to
the pitot block. The tubing had better
stay attached this time. Based on some
information found in the VanAirForce RV-12 forum I have increased the value to
120,000+. I will see if the actual fuel
used and the calculated amount come a little closer. I also used some Plexus to clean the bugs off
of the nose and wing. With everything
put back together, cleaned, safety wired and updated, the airplane is once
again ready to fly!
Monday, July 7, 2014
Airspeed Problems
I went to the airport this morning to try and
fly with the temps a little lower. I
made 3-take-off attempts before finally throwing in the towel. The head temps were in line, but the airspeed
indicator would not go above 48 knots.
Each time the airplane wanted to fly, but without 55 knots showing I
aborted each take-off. I taxied back to
the hanger and got out the PAP. I turned
to the pitot test page, hooked up a syringe and attempted to pressurize the
pitot tube. NO JOY!. Nothing shows on the airspeed indicator. I blew into the tube with the same
results. I removed the top cowl to find the
plastic pitot tubing had come off of the pitot tube at the pitot block. This explains why I was unable to get up to
55 knots on the 4th. Before
reconnecting the tubing to the pitot tube I rerouted it over the engine under
some hoses it had previously passed over so there is no tension on the
tubing. I think there may have been some
tension and that is why it became disconnected in the first place. I reattached the pitot tubing to the pitot
tube and safety wired the connection. I
also ran the twisted safety wire to the screw holding the pitot tube in the
pitot block and twisted it in place. I
ran a 1 minute test on the pitot system and it dropped less than 2 knots on the
airspeed indicator. Hopefully I will be
able to get back into the air on Friday the 11th.
Thursday, July 3, 2014
Took Grandkids Flying
Today was going to be a fun day taking 3-of
my grandkids for a short flight. I took
Taylor, my granddaughter up first. We flew
around the south end of the valley for about 20 minutes then returned to the
airport. We taxied to the hangar and I
shut off the engine. Taylor exited the
aircraft and Kaleb climbed in. I
restarted the engine and the oil temp was quite high. The cylinder heads were also very hot, over
240o. I taxied out to the runway and attempted a take-off. I could not attain a 55 knot airspeed with only 1500’ left on the runway so I
aborted the take-off. By then both CHTs
were in the red. I taxied back to the
hangar and shut it down for the day. The
OAT was 36c and there was a hot wind blowing.
I think shutting the engine down for about 5 minutes and then restarting
was too much for the cooling system. The
engine became too hot just sitting for that time, retaining heat instead of
losing heat. I am going to have to do
something about that if I am going to continue flying during the hot
weather. I have checked the VansAirForce
website and relocated some posts about a heat shroud between the muffler and
the oil cooler. I will be doing the 25
hour 1st oil change in the next few days and will see about
installing a shroud while the lower cowling is off.
Flight To Wendover and Wheel Pants
On July 1st I made a flight to Wendover and back. I took Tim, my grandson along as a
passenger. We had a pleasant
flight. The airplane performed well. After departing the Salt Lake Valley we
started our climb over the lake. We
climbed to 8500 and all went well. I was
climbing at 200 VS to keep the head temperatures down. It was a hot day, but we did just fine. After spending about 30 minutes on the ground
in Wendover we made the return flight.
It was nice to be able to fly out and back in about the same amount of
time it takes to drive one way.
I continue to have background noise on the
headset. The noise occurs when I am at
full throttle climbing out. It diminishes
when I am at cruise but really never goes away.
The noise begins with some popping sounds and then progresses until
there is a lot of static and it is hard to hear radio communications. It is most pronounced on the pilot
headset. I did some research and have
found some information that indicates a solution maybe to adjust the mic levels
on the SL-40. Yesterday I made the suggested
changes and plugged in my small shop vac.
I put the shop vac on the passenger seat, closed the canopy and turned
it on. This is one the tests another
pilot used to check the background noise being picked up by the mic. I called Unicom for a radio check and all
went well. I hope to get back into the
air to do a flight test.
Yesterday I installed the wheel pants and fairings. I also want to get back into the air to see
if there is a change in performance.
Everyone I have talked to about this suggests the performance will be much
improved.
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